A Novel Approach to Experimentally Create and Mitigate Head-in-Pillow Defects
One of the solder joint failures encountered frequently during Printed Circuit Board Assembly (PCBA) is due to Head-in-Pillow (HiP) defects. The primary cause of HiP defect is due to the warpage of the component during the reflow process. The ultimate solution for solving HiP is to eliminate component warpage however that is very difficult to accomplish in all packages due to various material and construction constraints. Hence,there is a need to find other approaches to solve this problem. One effective solution would be to investigate a solder paste that can mitigate HiP defects.
The theory investigated here presumes that had the BGA spheres maintain contact with the main card solder paste the HiP defect would not occur. Therefore it is during SMT reflow that package warpage raises the BGA sphere(s) up off the applied solder during flux activation and reflow. The BGA sphere only returns to contact the melted/coalesces solder paste during cooling when the package has begun to return to its initial flatness. At this point either the flux is exhausted and is unable to form the joint or the flux itself has created barrier between the two solder features,BGA sphere and PCB solder bump created from the reflow paste on pad.
The Head-in-Pillow defects parts per million (DPPM) level would require a DOE sample size in the thousands therefore this study devised a method to create Head-in-Pillow defect in a controlled lab environment. This method eliminates the use of expensive problematic BGA components and instead applies control over reflow conditions and timing of the contact between the solder ball and the melted solder paste. The SRT BGA rework machine was used to effect programmable control of the time and temperature profile and sphere contact timing.
A baseline SRT process was established using a solder paste common to multiply production line exhibiting HiP defects. The baseline profile was modified until the baseline solder paste consistently created HiP defects. Using these same programmed SRT parameters eight other no-clean solder pastes from different vendors were evaluated. A high resolution video camera was used to record the entire reflow process and track the occurrence of the HiP joint. The performances of all the pastes were analyzed to determine the best solder paste to mitigate HiP defects. The results of this study were incorporated into production and were further validated through the elimination of the HiP joint defect. This test method provides engineers a means to evaluate a solder paste effectiveness in mitigating HiP defects.